I'll keep the replacement option in mind, but it seems to be good after loosening the allen head screws about 1/3 of a turn.
Riding home Thursday it did a great job of helping me forget what a lousy day at work it was. Near home it started to sputter for a fraction of a second and I thought "now what?" and then realized the reserve setting would be the first thing to try. That was the only problem, so it looks to be on track for another tank of 40 mpg.